A Model 700 European

I like the Remington 700.  That’s been true for every one of the several Model 700s I’ve owned over the years, starting with a left-hand 30 06 BDL I bought in the late 1970s in Fort Worth, Texas.  I’m right-handed, but the price on that 700 BDL was too good to let it get away.  That rifle would put five shots of just about anything inside an inch at 100 yards.  One of my good buddies had a teenaged southpaw son who was looking for a rifle and that BDL found a home with him (and the following month he used it to bag a deer, so it was a win-win for everyone except Bambi).

Three decades later I saw the subject of this blog, a Model 700 European in 30 06, new in the box and I had to have it.  It had nice figure, it was unfired, and it was the rare European model.  The Remington 700 BDL normally came with a high-gloss urethane finish, but in the early 1990s Remington offered the rifle in limited quantities with a satin oil finish.  The European 700 BDL model was available in six chamberings:  .243, .270, .280, 7mm-08, 7mm Rem. Mag., .30-06 and .308.  I’ve never seen another European in any caliber.  In 1994, the second and last year of production, the Model 700 European listed for $524.

I kept the rifle for about 10 years without firing it, taking it out of the safe to admire it occasionally.  There were a couple of things I didn’t like about the rifle.  Remington apparently put only one coat of tung oil on the stock, and the wood was fairly porous.  I knew that the stock would be a magnet for moisture in that condition.   And, the inletting around the floor plate was sloppy…it touched the metal on one side and had gaps on the other.  I needed a project, and the Remington European 700 BDL was it.  I glass bedded the action (and the trigger guard/floor plate area) and I went to work on the stock by adding 10 coats of TruOil.  Then I found a good load for this rifle using IMR 4166 propellant (that blog is here).

As I added each coat of TruOil, I keep flipping back and forth between leaving a gloss finish on the rifle or knocking it down with 0000 steel wool.  I liked the look of the gloss finish, but I liked the satin finish better.  I think this one turned out well.

The Model 700 European with seven coats of TruOil, each one polished with 0000 steel wool and wiped clean before applying the next coat.
After the ninth coat of TruOil, I was just about there. Ten coats would finish the rifle.

It’s easy enough to put another coat of TruOil on if I want to return to a gloss finish, but for me, the satin look is much more elegant, and that’s what I went with.

Load testing with the glass bedded and refinished Model 700 European.
Three shots in under an inch. It will do that with five shots, too, but it’s hard to get game to sit still for five shots.

I’m going to sell the European (through an FFL, of course).  I have other toys and the European BDL doesn’t fit the rest of my collection.  It’s a sweet shooter and it needs a good home. If you’re interested, drop me a line at info@exhaustnotes.us.

IMR 4166: A quick look

Necessity is the mother of invention, or something like that.  When I heard that IMR 4320 was discontinued (on top of the ammo and components shortage), I was not a happy camper.  IMR 4320 was my go to powder for several cartridges, and now what I have left is all there is (and it’s almost gone).  But it really doesn’t matter, because we can’t hardly find propellants of any flavor. That notwithstanding, I made the trek to my local components supplier a couple of weeks ago, and he had only three propellants left:  IMR 4166, 8208, and BLC2.  I’ve never used any of these, although I had heard of Ballsy 2.  The 4166 seemed interesting…it matched my motorcycle jacket, but none of my reloading manuals had any data for it (it’s that new).  I bought all three.

I went online and found data published by the manufacturer, so I worked with that for my 30 06.  IMR 4166 is an extruded stick powder.  It will flow through a dispenser, but the dispenser throw variability was about 0.2 grain, and that’s enough when loading for rifle accuracy that I’ll weigh every charge with my scale and trickle it in with my RCBS powder trickler.N Would 0.2 grains make an accuracy difference?  I don’t know (and someday I’ll test to find out).  I suspect not, but weighing every charge only takes a few seconds more, and it seems like the right thing to do.

IMR 4166 is a stick powder that looks like any other stick powder. It’s in a powder trickler in this photo. Yeah, I weigh the powder for every cartridge.

On the IMR website, it said that Enduron IMR 4166 is one of a new class of propellant that offers four adventages:

Copper fouling reduction.  These powders contain an additive that drastically reduces copper fouling in the gun barrel. Copper fouling should be minimal, allowing shooters to spend more time shooting and less time cleaning a rifle to retain accuracy.   Hmm, that might be interesting.  We’ll see how it does, I thought to myself as I read this.

Temperature change stability.  The Enduron line is insensitive to temperature changes. Whether a rifle is sighted in during the heat of summer, hunted in a November snowstorm or hunting multiple locations with drastic temperature swings, point of impact with ammunition loaded with Enduron technology will be very consistent.  In the old days, I might have dismissed this as a solution looking for a problem, but I’ve experienced what can happen in a temperature sensitive powder.  I had a max load for my 7mm Weatherby that was fairly accurate that I took out to the range one day when it was 107 degreees.  I fired one shot and had great difficulty getting the bolt open.  It’s a real issue if you develop a load at one temperature and then shoot it at an elevated temperature.  If IMR 4166 is free from that characteristic, that’s a good thing.

Optimal load density.  Enduron powders provide optimal load density, assisting in maintaining low standard deviations in velocity and pressure, a key feature for top accuracy.   Eh, we’ll see how it does on paper.  I have some loads that are low density (i.e., they occupy well under 100% of the case volume) and they shoot superbly well.   I’m interested in how the load groups.  The target doesn’t give extra credit if an inaccurate load has a low standard deviation.

Environmentally friendly.  Enduron technology is environmentally friendly, crafted using raw materials that are not harmful to the environment.  Okay, Al Gore.  Gotcha.  Now go back to inventing the Internet.

My test bed for the new powder would be a Model 700 Euro in 30 06, a 27-year-old rifle I bought new about 10 years ago.  I had just refinished it with TruOil and glass bedded the action (a story a future blog, to be sure), and I hung a cheapie straight 4X Bushnell scope just to get a feel for how everything might perform.

The Model 700 Euro had a tung oil finish. The rifle was only offered in 1993 and 1994. The tung finish didn’t do it for me, so I did my usual TruOil finish. That’s an old Bushnell 4X economy scope up top.

My load was to be a 180-grain Remington Core-Lokt jacketed soft point bullet and 47 grains of the IMR 4166, all lit off by a CCI 200 primer.  If you’re interested, I was using Remington brass, too.  The cartridges were not crimped.

Loaded 30 06 ammo with the Remington 180-grain jacketed soft point bullet.

Wow, those 180-grain bullets pack a punch.  Recoil was fierce, and I probably felt it more because the Model 700 doesn’t have a recoil pad.

Okay, that’s enough about my heroics.  Let’s take a quick look at how the propellant performed.   With regard to the reduction in copper fouling claim, I’d have to say that’s an accurate claim.  After 20 rounds (the very first through this rifle), I ran a single patch with Hoppes No. 9 though the bore, followed by a clean patch, just to remove the powder fouling.  There was a very modest amount of copper fouling, way less than I would have seen with any other propellant.  Ordinarily, at this point in the cleaning process (i.e., removing the soot) I would normally see a bright copper accent on top of each land.  With 4166, there was only a minimal amount of copper present (as you can see below).   After a second patch with Hoppes No. 9, the copper was gone.  I guess this copper fouling eliminator business is the real deal.

This is a brand new rifle even though it’s nearly 30 years old. Check out the machinings inside the bore. Remington, for shame!

With regard to accuracy, 4166 has potential.  I shot five targets that afternoon, and this was the best.  It’s a 0.590-inch group at 100 yards, and that ain’t too shabby.

Sometimes you just get lucky. Other times you rely on careful load development, glass bedding, and a steady trigger squeeze.

The bottom line for me is that IMR 4166 is a viable powder.  Now, like everyone else, I need to find more.  That’s going to be a challenge.  But at least I know that my IMR 4320 has a decent replacement.

Refinishing the Mini 14

A couple of years ago I spotted a beat-up old Mini 14 rifle stock in the used parts junk pile at my favorite local gunstore, and I thought it might be fun to refinish it.  It was for the earlier series Mini 14 and I didn’t own one, but the stock looked like it needed me.  It was dinged up but didn’t have any gouges, and the anodized aluminum buttplate had multiple scratches.  I asked John, the guy behind the counter, what he wanted for the stock, and we were both in a quandary.  John’s brow furrowed.  He was searching for a price that wouldn’t be insulting, but I could see that he was eager to unload something that had all the earmarks of becoming a permanent resident.  There were several old timers in the shop (there always are; it’s that kind of place).  All eyes were on John and me.

“I don’t know…maybe $25?” John said.

I recoiled as if struck by an arrow.  It’s all part of the game, you know.   All the eyeballs were on me now.  It was like being in a tennis match.

“I don’t know, John,” I answered.  “I was going to offer $30, but if you gotta have $25, then $25 it is…”

Everybody laughed and I went home with a Mini 14 stock that looked as if it had been to Afghanistan.  I wished I had the foresight to grab a few “before” photos of it, but I did not.

Like I said, the stock was decrepit, but I wanted a refinishing project and now I had one.  I removed all the metalwork, I stripped the finish (you can see how to do that in our series on the Savage 340 refinish), I steamed out the dents (same story there; it’s covered in the Savage 340 stock refinish series), and then I went to work on it with 200, 320, 400, and 600 grit sandpaper.  The buttplate was hopelessly scratched all to hell, so I did the same thing with the same grades of sandpaper and I decided to leave the aluminum bare.  In one of my prior aerospace lives, I worked at company that made interior doodads for aircraft, and the approach I just described was one we frequently used for doorknobs, latches, and the other metal chotchkas you see in aircraft cabins.  That particular company was not a good place to be (my boss was a butthead), but I liked working with the crew of Armenians who handled all of our finishing work.  Whenever I had an idea about making an improvement, those guys were quick to tell me that wasn’t how they did it in the old country, and I went with their expertise (it was the right thing to do).  But I digress; that’s a story for another time.

Mini 14 stocks are birch, which is a light wood, and the question was do I want to stain the birch for a darker look, or leave it unstained for a lighter look?  I went for Door Number Two, and I think it turned out well.  I used the same approach described in the Savage 340 blog, taking care to use very light coats applied with a fresh bit of T-shirt cloth each time and waiting a day between applications.  This one has 10 coats of TruOilTruOil is good stuff.

I had a beautiful rifle stock, but no rifle to go with it.  One of my good buddies told me his brother had a Mini 14 that was in rough shape, so I gave the refinished Mini 14 stock to him to send to his brother.  It was a fun project and I really liked the way this one turned out.


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